Leaky Sea Water Pump
When we got the boat, the starboard engine always had a hard time priming the sea water. I thought I had a leaky hose, but couldn’t find it. No leaks coming in, but the pump must be sucking air now and again. Finally it got bad enough where I could actually see water coming in. The seal of the pump was bad. I had a spare so I changed it out. That was about a month or two ago. I ordered a rebuild kit for the old pump. It was half the price of a new pump, so by rebuilding it, I can have another spare pump on the cheap, well cheap is a relative term when it comes to boat parts.
Rebuilding the Yanmar salt water pump is pretty easy. The most helpful tool to me is the parts breakdown picture. It helps me to verify that all the parts are going back together the right way. If you don’t have the parts book, possibly the parts counter guy can copy the page for you. If you can’t get that, then I suggest taking photos while it’s coming apart as well as lining up the parts as they come out.
Removing the back cover exposes the impeller; it just pulls off maybe with a little tug and with a needle nose. If the impeller is still in good shape and will be stored for any length of time, it should be put in a Ziploc bag with glycerin. The factory guys will tell you that you can use olive oil instead (not many people have glycerin). That will keep it soft and stop it from drying out. There’s nothing like a soft, supple impeller.
After the impeller comes off, the pump needs to be turned around. The pulley can come off with the turn of a nut. Next there’s a retaining clip that can come out. They make special tools for these, and I thought I had one, but can’t seem to find it. So I resorted to the tips of a needle nose. Once it pulls out the shaft with both bearings can be tapped out from the impeller end. Make sure you use a soft block of wood or plastic. You don’t want to damage the shaft end.
After it’s out, the large bearing needs to get tapped off. I like to use a bearing puller for this, but don’t have one. So an open ended wrench that just barely fits around the shaft worked. I put that between the bearings and tapped the shaft with a hammer (first I put the pulley nut back on to protect the threads). I couldn’t get the bearings off the shaft. I resorted to drastic measures: a ride to the hardware store. I wanted a vise, but one that was portable and light. I found a Stanley that fit the bill and made the job much easier. It held the wrench and bearing while I tapped the shaft, viola, the bearing was off.
Next there’s another clip holding in the smaller bearing, taking this off and some more tapping and I was left with the shaft. I used some ultra fine emery cloth to polish this up and get it ready for the new bearings. Once clean, I pressed (tapped) the new bearings on in reverse order. When doing this, one thing to keep in mind is the bearings are intricate pieces of machinery. I like to use a small hard tube or pipe that is the exact size of the inner ring of the bearing. I put that on the bearing and tap it down. When tapping the bearing into place, don’t put pressure anywhere but the inner ring; otherwise you risk damaging the bearing and causing premature failure.
In the pump housing was left the seal, an o-ring, and a plastic piece. I took these out, being careful not to damage the bronze housing. Cleaned everything up and got ready to put it back together.
I lubricated the seal and shaft with glycerin to help slide the shaft in without causing damage to the seal. I then tapped the shaft with the bearings gently into place (still with the old pulley nut protecting the threads. Put the nuts and pulley back on and it was ready. I spray painted it quickly and let it dry. Just like new!
Because I’m using this as a spare, I left the impeller and back cover off. This will stop the impeller from getting damaged by staying in one position to long. They can go in easily and then the pump can be installed when needed.
It didn’t take much time at all, an hour or an hour and a half at most, and now I have a spare that is easily changed out in case of a failure. More importantly I know a little more about the engines and systems on the boat, making us a little more self-sufficient. Oh and I saved some money in the process.
All in all, a productive morning.






















What do we have? I’ve been running our refrigerator and freezer for several weeks now and every day the batteries have been 100% charged before lunch. I know we’ll be using more energy once we’re on board, but those are the two biggest energy hogs that we have. Well I will be on board with 4 women, so we’ll just have to see if that fact stands. At least the women don’t look like pigs.

